FOR OFFICIAL USE
(No. 7887.)
AUXILIARY MOTOR KETCH "XL."
THE MERCHANT SHIPPING ACT, 1894.
REPORT OF COURT.
In the matter of a Formal Investigation held at the Institution
of Civil Engineers, Great George Street, in the City of
Westminster, on the 12th, 13th, 14th and 29th days of May, 1931,
before Herbert Metcalfe, Esq., one of the Magistrates of the Police
Courts of the Metropolis, assisted by Captain J. Elmes, Captain W.
A. Splatt and T. H. Blaker, Esq., as Assessors, into the
circumstances attending the loss of the auxiliary motor ketch "XL"
of Castletown, in the Isle of Man, on the 5th day of July, 1930, in
the Firth of Clyde.
The Court, having carefully inquired into the circumstances
attending the above-mentioned shipping casualty finds, for the
reasons stated in the Annex hereto, that the loss of the vessel
"XL" was caused by the flooding of the vessel with sea water.
The Court is satisfied that the entry of this water was not due
to the alleged contact of the vessel with any floating and/or
submerged object, but that the water entered through some aperture
in the after part of the vessel on the 4th and 5th July, 1930.
The conduct of William Bruford Stokes, as part owner, in the
matter of the insurances effected upon and in the financial affairs
of the vessel, his conduct when he was acting as mate, and also the
conduct of John Borman Goff, who was master at the time the vessel
was making water on the 4th and 5th of July, 1930, was such that
there is the gravest suspicion that the "XL" was deliberately
scuttled, but in the absence of any evidence other than that of the
crew, which was most contradictory and unsatisfactory, the Court is
unable to find this as a fact.
The Court finds that John Borman Goff, master (Certificate Home
Trade No. '106786), was in grave default in not taking the
necessary steps to save the vessel when she was making water on the
4th and 5th of July, 1930, and his certificate is ordered to be
suspended for a period of six months from this date.
The Court also finds that William Bruford Stokes (who is
uncertificated), mate and part owner of the "XL", was also in grave
default and he is most severely censured and ordered to pay the sum
of Twenty Pounds (£20) toward the costs of the Inquiry.
Edith Stokes, the registered managing owner, is absolved from
all blame.
Dated this 29th day of May, in the year 1931.
HERBERT METCALFE,
Judge.
We concur in the above Report.
| | John Elmes,
W. A. Splatt,
T. H. Blaker, | Assessors. |
ANNEX TO THE REPORT.
This Inquiry was held in the Council Chamber of the Institution
of Civil Engineers in Great George Street, in the City of
Westminster, on the 12th, 13th, 14th and 29th days of May, 1931,
before Herbert Metcalfe Esq., one of the Magistrates of the Police
Courts of the Metropolis, assisted by Captain J. Elmes, Captain W.
A. Splatt and T. H. Blaker, Esq., as Assessors.
The object of the Inquiry was to ascertain the circumstances
attending the loss of the auxiliary motor ketch "XL" of Castletown,
Isle of Man, on the 5th of July, 1930, in the Firth of Clyde.
Mr. G. St. Clair Pilcher (instructed by the Solicitor to the
Board of Trade) appeared for the Board of Trade. The other parties
to the Inquiry were Captain William Bruford Stokes, of 6,
Summerdale Avenue, Milton, Weston-Super-Mare, his wife, Edith
Stokes, of the same address, Captain John Borman Goff, of 69,
Botanic Road, Liverpool, Charles Chapman, of 2, Albert Terrace,
Church Street, Highbridge, Somerset, and John Robert Buller Meek,
of 6, Bow Street, Maryport, all of whom appeared in person and were
not legally represented. All the parties admitted having received
the requisite notices of the Inquiry as required by the Shipping
Casualties and Appeals and Re-Hearings Rules, 1923, dated May 4th,
1923 (S.R. and O. 1923 No. 752/L.9). There were no other
parties.
The "XL", official number 67284, was a British built sailing
ship with an auxiliary motor, registered at the Port of Castletown,
Isle of Man. She was stoutly constructed of wood, carvel built, at
Port St. Mary, Isle of Man, in 1873, by one, Joseph Qualtrough. She
had one deck, with two masts rigged as a ketch. Her dimensions
were: length 74.2 ft., breadth 19.4 ft., depth 9.2 ft., with a
gross tonnage of 74.6 tons, giving a register tonnage of 52.83
tons. She was divided by wooden bulkheads into a forecastle used
for the crew's accommodation, a boatswain's store, a main hold and
abaft the main hold was an engine room and then, further aft, the
master's cabin. Originally constructed as a sailing ship, she was
fitted in 1919 with two auxiliary, 4-cylinder Kelvin internal
combustion engines, each operating one propeller shaft. She was
acquired in 1926 by one, Arthur Llewellyn Coffey of Ramsey, Isle of
Man, and used by him for some time, but was later laid up and
advertised by him for sale. She was sold by Bill of Sale dated 29th
April, 1930, to William Bruford Stokes, who was acting on behalf of
his wife, Edith Stokes, of 6, Summerdale Avenue, Milton,
Weston-super-Mare, for the sum of £130, and at the time of her loss
Edith Stokes was registered and designated as her managing owner.
The circumstances of her acquisition were rather out of the
ordinary. W. B. Stokes (known as Captain Stokes, though he had no
certificate of competency) in answer to the advertisement in April,
1930, went to the Isle of Man with Captain J. B. Goff and Charles
Chapman and lodged with the then owner of the "XL", Mr. A. L.
Coffey. Goff held a master's certificate of competency, No. 106786,
Home Trade, and was well known to Stokes and had sailed with him in
another small vessel which had also been lost at sea. Chapman was
half-brother to Stokes, and had likewise sailed both with Stokes
and Goff on similar occasions.
Stokes paid Coffey the sum of £80 for the hull of the "XL" and
Coffey fitted for him one auxiliary motor, a 20 h.p. Clyde engine
operating one propellor shaft on the starboard side, for the
additional sum of £50, a total of £130. The remaining propeller
shaft tube had been closed previously, whilst the boat was in use
by Coffey. When the boat was fitted with two engines, two
circulating pumps, each with an inlet pipe of ¾ inch in diameter
into the engine room, had been fitted for use with the Kelvin
engines. When the Clyde engine was fitted these two inlet pipes,
which were each fitted with a lever cock, remained in position, one
being connected by a rubber pipe to the Clyde engine and the other
tube was plugged on the inside although the cock remained in
position. Further expenditure was necessary to fit the vessel for
sea, and, so far as can be ascertained, a total sum of £162 2s. 9d.
was spent by Stokes for this purpose at Ramsey.
The "XL" had been surveyed in January, 1929, by a Board of Trade
surveyor, and certain of his recommendations had been carried out
by Coffey before the vessel was advertised for sale. She was again
surveyed by the same surveyor on the 19th May, 1930. Certain
recommendations were again made. These were" not opened out
"surveys, and when Coffey wished to sell the vessel to Stokes all
the work required to be done by the Board of Trade surveyor was
carried out by Coffey on behalf of Stokes and to the satisfaction
of the surveyor.
The total cost of this work done by Coffey on behalf of Stokes
was £69 18s. 1??d., of which sum £14 10s. 4d. is still owing to
Coffey.
It is of interest, having regard to future events, to remark
that Coffey told the Court that when he was about to give Stokes
the receipt for the £130 he was asked by Stokes to make out the
receipt for £400. Coffey demurred and enquired the reason of such a
curious request and was told by Stokes that it would be better for
him (Stokes), but Coffey refused and the receipt was made for the
£130 only.
The money for the purchase of the "XL" was found by Mrs. Edith
Stokes, who negotiated a mortgage on her house at Milton for the
sum of £270 with Barclays Bank where she and her husband had a
joint banking account. This money was given to Stokes by his wife
and he acted throughout as her agent, and although Mrs. Stokes was
designated and registered as the managing owner of the "XL" she
never saw the vessel and knew nothing of the circumstances of the
loss nor any of the financial transactions concerning the vessel.
When the "XL" was lost a sum of £300 was paid to Stokes by the
underwriters but Mrs. Stokes was apparently unaware of this and the
mortgage is still outstanding. Except that Mrs. Stokes provided the
money and as registered, unknown to herself, as the managing owner
the Court was satisfied that she had nothing to do either with the
conduct of the affairs of the vessel or with its loss, and
discharged her from the Inquiry.
The "XL" left Ramsey on the 4th June, 1930, light, for Maryport
with William Bruford Stokes as master, John Borman Goff as mate and
Charles Chapman as A.B. She was in good and seaworthy condition and
although fitted with an auxiliary motor she was primarily a sailing
ship. The motor from its subsequent history cannot be said ever to
have been reliable, and having regard to all the circumstances this
lack of reliability cannot be said to have had any influence on the
loss of the vessel. The motor was entirely auxiliary and no
circumstance arose in which an entirely reliable auxiliary engine
would have altered the situation, and accordingly in dealing with
the history of the "XL" after she left Ramsey the Court have
regarded her as primarily a sailing ship. On arrival at Maryport
the engine needed attention and the bulkhead of the engine room was
slightly altered in order to allow easier access to the starting
handle. One of the local men, John Robert Buller Meek, who was
employed on this work, was engaged as A.B. and motorman for the
remainder of the voyage. A cargo of coal was loaded and the "XL"
proceeded to Drummore with a crew of four under the command of
Captain Stokes. This cargo of coal was discharged at Drummore and
the vessel then went on, light, to Ayr where she arrived on 22nd
June, 1930. Stokes had been ill since the vessel left Ramsey and he
said that he desired to be relieved of the responsibility of the
command. He certainly had been ill, but judging from his subsequent
conduct, the illness does not appear to have been of such a nature
that he was unable to take an interest in the affairs of the
vessel. His subsequent conduct shows that, far from being unable to
think clearly, he was able to draft remarkably clear letters on the
question of the ship's insurance to the underwriters. As a matter
of fact he did hand over actual command to his mate, J. B. Goff,
who was appointed master and Stokes re-signed as mate. Stokes said
that he desired to remain in the vessel in order to get a cheaper
journey from a port near his home in Somerset and so save the
railway fare. The vessel in fact next called at Lamlash and Meek
said that before leaving Lamlash he was told by Stokes to pack his
bag as it was Stokes's intention to leave the vessel at Stranraer.
It is of interest that it was from this place that Stokes did
eventually return to Somerset. Goff said that it was their
intention to go to Kilkeel, thence with a cargo to Liverpool, and
then if possible to get another cargo to Bridgwater, which was
quite close to Milton: Chapman was doubtful of the intention of
Stokes in this matter but it is apparent that there was no great
urgency and that Stokes had no fixed intention to leave the ship at
any particular place or time.
At Ayr the "XL" loaded a cargo of 106 tone of coal consigned to
William Annett of Kilkeel, Co. Down, and left Ayr for Kilkeel on
the 26th June, 1930, under sail and motor. At this time there was
on board a reserve supply of about one gallon of lubricating oil
and, having regard to the auxiliary nature of the engine, this
supply might have been sufficient for the intended voyage, but part
of this oil was lost by the accidental upsetting of the can by Meek
soon after leaving Ayr. This loss was reported both to Stokes and
Goff and the supply was never replenished. The vessel left Ayr with
the benefit of a W.S.W. breeze, a wind which would have been quite
favourable for the voyage to Kilkeel, but for some reason
unexplained to the Court her course was altered and she made for
Lamlash, a direction quite unfavourable with a W.S.W. wind. At
Lamlash further attention was given to the gearing and timing of
the engine by a Mr. Alexander Hamilton at a cost of 20s. and this
sum is still owing to Mr. Hamilton; a minor matter, except perhaps
for Mr. Hamilton, but it is an indication that the supply of money
in the boat was not great. The "XL" stayed at Lamlash for some days
and finally left that port about 7.0 a.m. on the 4th July, under
sail and motor with her small boat in tow. The evidence of the
position of the small boat was contradictory but the Court is
satisfied that the boat was in tow and was never again taken
inboard and placed on the after hatch-its usual resting place.
There was no good reason why it should not have been taken inboard;
it was a task more easily undertaken in harbour than when at sea
and the Court does not accept the evidence that at a later time it
was taken in.
Leaving Lamlash the weather was fine, the wind being variable
from S. to S.W. and W., force from calm to force 3, with good
visibility and a smooth sea. Except for slight patches of fog later
in the day there was no appreciable change in the weather
conditions from the time the vessel left Lamlash until she
foundered some twenty hours later. Her course was set S.S.W. for
Corsewall Point and although she left making from three to four
knots she apparently made little progress, being only about four
miles E. of Pladda by about midday when the motor was stopped. Meek
the motorman said that this stoppage was due to shortage of
lubricating oil, a fact that he again reported to both Stokes and
Goff, but it was an unreliable engine and the ship was probably
making way under sail at a speed equal to that which could be given
by the motor and the Court does not attach any great importance to
the behaviour of the engine.
The Court found much difficulty in ascertaining the exact course
of events after the vessel passed Pladda. All the four members of
the crew later, at different times and places, made sworn
depositions before Receivers of Wreck and their depositions were
available for the Court. All the crew gave evidence before the
Court and in some cases amplified and in other cases denied and
altered the statements they had made in their depositions. The
whole evidence was such that the Court is satisfied that the loss
of the "XL" was not a genuine misfortune of the sea. The Court
finds as a fact that at about 4.45 a.m. on the 5th July, 1930, the
"XL" foundered about two miles from Ballantrae in fine weather and
that the whole crew, fully dressed, came ashore some half hour
later in their own boat bringing with them a bag and also a tin
box, the latter being the property of Stokes, and that none of the
ship's papers except the official log was saved. According to the
master, Goff, there was at least two hours from the time she was
first making water until they took to the boat and that they stood
by the vessel for half an hour before she sank, and had there been
any real desire to save the papers there was ample opportunity for
it to have been done.
The first deposition was that of Goff, the master at the time of
the loss, made on the 5th July, 1930, a few hours after the vessel
foundered, before the Receiver of Wreck at Stranraer. Goff said
that at about 2.0 a.m. on the 5th July, whilst he was at the
wheel-in hazy weather-wind force 2-tide slack-he felt a sharp
impact forward and sent Charles Chapman, the A.B., to investigate
the cause. Chapman returned in a very short time and reported that
the timbers on the bluff of the bow, inside the forecastle, had
been pierced and that the ship was making water rapidly. He called
all hands and manned the pumps but they were unable to cope with
the inflow of water-the wind fell away-they were unable to beach
her as she became unmanageable and about two hours after the first
alarm they took to the boat and stood by until she sank about half
hour later. He said that all flares were burned but with no
response. None of these flares appears to have been seen and the
Court is unable to say definitely if in fact they were or were not
shewn, as the coastguard at Ballantrae was not on watch, the
weather being fine, and it is possible that had the flares been
shewn they might not have been seen.
Stokes made his deposition on the 15th October, 1930, some three
months after the loss and during this time he had been in conflict
with the underwriters on the question as to whether or not he had
been justified in insuring the vessel for the amount which he had
claimed from them. In his deposition he said that he was asleep in
the master's cabin aft. He had continued to use this cabin even
though he was only aboard as mate. He said that he was awakened
about 1.0 a.m. on the 5th July by Goff, who told him that the
vessel had struck something and was making water rapidly, so much
so that Goff enquired of Stokes as to where he could beach her.
Stokes continued in his deposition to say that he decided to run
for Ballantrae and then went to the wheel for that purpose whilst
the rest of the crew worked the pumps but were unable to cope with
the water. Stokes did not see the alleged damage himself.
Charles Chapman, the A.B., made his deposition on the 18th
October, 1930, and in it he said that during the afternoon of the
4th July the ship struck something and he saw water coming into the
engine room; going forward to investigate he found in the
forecastle, some 18 inches below the water line, a hole in the
lining or ceiling on the starboard side, large enough to put his
fist through.
Meek did not make his deposition until the 10th November, 1930.
His association with the other parties only commenced when the "XL"
had reached Maryport and he had no financial interest in the vessel
and knew nothing of her affairs. In his deposition Meek said that
when the engine was stopped on account of the shortage of oil in
the early afternoon of the 4th July it was a fine summer day and he
went to sleep on the after hatch where the small boat was kept when
it was inboard. After he had been asleep for about two hours he was
aroused by Chapman who told him to turn in in the forecastle; he
did so and again went to sleep. He was again aroused some hours
later again by Chapman, it being still daylight, and was told by
Chapman that the vessel had struck something and was making water.
Meek said that he lifted a board in the forecastle floor and saw
water underneath in the forepeak. This water was not then level
with the floor. Meek then went on deck and going aft saw water in
the engine room almost as high as the crank case. He started up the
engine but it stopped soon afterwards when the water reached the
carburettor.
In his evidence before the Court, Meek, who had been consorting
with the other parties since the commencement of the Inquiry, tried
to nullify the effect of the divergence of his deposition from
those of the other parties, particularly those of Goff and Stokes,
on the plea that he was drunk when his deposition was taken by the
Receiver of Wreck. The Court has no hesitation in rejecting this
plea of drunkenness and is satisfied that no Receiver of Wreck
taking a deposition at the special request of the Board of Trade
would ever take such a deposition if there was any sign that the
deponent was either under the influence of drink or from other
reasons unable to appreciate the nature of his act, and that Meek
had other reasons for his desire to change his mind in this
matter.
It is interesting at this stage to compare the various
statements in the original depositions.
Goff and Chapman speak of the vessel striking an object with
force sufficient, according to both of them, to pierce the timbers
of this well made ship in the bluff of the bow, constructed with an
outer skin of 3 inch pitch pine planking supported by 5 inch by 7
inch oaken frames with a space of not more than 6 inches between
them and lined on the inside with planking over 1 inch thick, to
such an extent that on the inner side of the forecastle on the
starboard side 18 inches below the water line there was a hole
large enough for Chapman to put his fist through. Goff suggested
that the hole on the outer side was even larger and that probably a
piece of the outer skin had been forced away. The blow necessary to
cause such an injury must have been very severe, having regard to
the state of the weather and the probable speed of the vessel, but
whatever the nature of the alleged blow may have been it was not
felt by Stokes in the after cabin, and was not sufficient to wake
Meek, who was asleep in the forecastle in a bunk on the starboard
side in a position which would have been flooded almost immediately
had the story of Goff and Chapman in this respect been true. Meek
said that he knew nothing of any such injury to the vessel and the
first indication which he received of the presence of water was
when he was roused by Chapman in the forecastle.
Chapman said that on his way forward to rouse Meek he saw water
coming into the engine room. Meek also said that after he had
lifted the board in the forecastle floor and seen water underneath
he also went aft and saw water in the engine room.
That there was water in the engine room and the vessel, when
Meek was roused, the Court has no doubt but it rejects entirely the
story that this water entered in the way alleged by Goff and
Chapman. The alleged hole in the forecastle was of a size
sufficiently large to destroy the whole of the reserve buoyancy of
the vessel by the filling of the forecastle within half an hour of
its making. No effort of any kind was made to stop the alleged leak
and the pumps were never efficiently brought into operation. The
two pumps were 5 inch deluge pumps and three able bodied men were
available to work them. One man was sufficient for each pump and
these pumps should have been ample to cope with the inflow of water
sufficiently long to enable the vessel to be beached. There was no
reason why an effort should not have been made to stop the leak.
The sea was calm and the breeze slight and the hole was according
to Goff and Chapman only 18 inches below the water line; Stokes was
at the wheel and the vessel did not become unmanageable for some
two to three hours after the occurrence. When it did become
unmanageable the crew took to the boat and stood by for about ½1/2
hour before she sank. Sufficient time was found to save a seaman's
bag and also a tin box which was the property of Stokes, but there
was apparently no time to save all the papers referring to the ship
and her affairs, although these papers were supposed to be in a
drawer beneath the bunk in the master's cabin at the after end.
The hours of darkness early in July in fine weather are not very
long and it was estimated that if water had been entering the
vessel only by way of the two cocks in the engine room sufficient
water would have entered in from 7 to 8 hours to destroy all the
reserve buoyancy. Water entering by this means would, owing to the
build and trim of the vessel, flow forward through the partition
between the engine room and the hold and along the bilges into the
hold and the forepeak. Chapman saw water coming into the engine
room at a time which according to him and to Meek was late in the
afternoon of the 4th July but still daylight, probably, having
regard to the time that Meek was asleep, somewhere between 6 and 8
p.m. Meek also saw water in the engine room about this time and the
Court is of opinion that the story as told by Chapman and Meek
concerning the time when water was first seen in the vessel is
probably true, and also that water was in fact entering the vessel
from the after end where it was first seen. The Court without any
doubt rejects the story of the alleged damage in the
forecastle.
Goff, the holder of a master's certificate, was the only
certificated man on board and the Court finds that his neglect to
use the pumps properly and to make any effort to stop the alleged
leak, which according to him was in an easily accessible position,
shows that there was no real desire on his part to prevent this
vessel from foundering.
It is now relevant to state the financial affairs of this
vessel. When the "XL" left Ramsey she was insured by Stokes in his
own name with the Union Marine Insurance Company of Liverpool for
the sum of £400. Stokes had effected this insurance through Messrs.
Coppack Bros. of Connah's Quay, Flintshire, who acted through
Messrs. Tyson Bros., ship brokers, of Liverpool. The vessel had
cost £130 for her hull and engine, and, in addition, there had been
spent on repairs and equipment at Ramsey a further sum of £162 2s.
9d. At Maryport the cost of the alteration to the engine room
bulkhead and the adjustment of the engine, etc., had cost
approximately £10, so that the total expenditure on the vessel was
£302 2s. 9d., over £90 less than her insured value.
Mr. Thomas Coppack, a member of the firm of Messrs. Coppack
Bros., produced to the Court the original letters and telegrams
from Stokes and copies of the letters from their firm and Tyson
Bros., etc., which were exchanged between them concerning the
insurances, etc., effected upon the "XL." On the 18th June, 1930,
Stokes wrote from Drummore to Messrs. Coppack Bros., "As I have had
to lay out a further considerable sum of money on her will you
kindly cover her in future for £600 instead of £400. Will you
please cover her now for a round voyage Drummore to Ayr, light, and
Ayr to Kilkeel loaded?" This order to increase the insurance was
accepted and confirmed. The next item of interest was a telegram
dated 5th July, 1930, from Stokes to Messrs. Coppack Bros. from
Ballantrae," Beg to advise you vessel "XL" foundered off Ballantrae
Ayrshire this morning striking submerged object."
The underwriters made enquiries and engaged the services of the
Liverpool and Glasgow Salvage Association, and, as a result of the
report which they received, the underwriters were satisfied that
the salvage of the vessel was not a satisfactory financial
proposition owing to her age and the depth of the water in which
she was lying. Stokes applied for the insurance money to be paid to
him and in a letter from him to Messrs. Coppack Bros. he said, "I
have kept the vessel insured from the beginning in accordance with
the instructions of the managing owner (his wife Edith Stokes) who
is very sorry to hear of the disaster but is pleased to know that I
carried out her instructions and kept her insured, as it turned out
a very wise thing as it happened. I was coming home and left her to
Captain Goff who was then in charge...."
The underwriters were not satisfied and were not disposed to pay
without further particulars, and referred the matter to their
claims adjuster having regard to the increase of the insurance at
Drummore. Messrs. Coppack Bros. on the request of the claims
adjuster asked Stokes to account for this increase in the insurance
from £400 to £600, and on the 26th July Stokes replied and, amongst
other things, said "the cost of the work done (at Ramsey) amounted
to between £470-£500. The receipts for the work were in the boat
when she went down and cannot therefore be produced. The vessel was
underinsured on her first voyage." On the 6th August in answer to
the request of the claims adjuster for copies of the receipts
referred to in his letter of the 26th July Stokes said, "I have no
note or recollection of the names of those who carried out the
work, in some instances there were no receipts as they were cash
transactions and in the others the receipts had gone down...."
Stokes threatened that in default of a speedy settlement he would
place the matter in the hands of his solicitors-a threat which was
never carried out! His reply of the 6th August was considered very
unsatisfactory and the insurers declined (to accept liability
particularly owing to the absence of information regarding the
repairs which were said to account for the lift in value. Stokes
offered to interview the underwriters' agent but they said that an
interview without the production of the necessary receipts would be
useless. Stokes however did call with Goff upon Messrs. Coppack
Bros. at Connah's Quay and Messrs. Coppack Bros. made it perfectly
clear to him that nothing but "bona fide" receipts or certified
copies thereof would satisfy the underwriters. Stokes in his
evidence tried partly to justify the lift in value on the ground
that he had ordered from Maryport a new set of sails at a cost of
£130. This order was in fact never accepted nor carried out by the
maker as he refused to do the work except on a "cash with order"
basis.
Stokes did produce certain minor accounts but these referred to
the original valuation and he could not produce any receipt or copy
thereof which would in any way justify the alleged rise in value.
In September he asked that some payment might be made to him on
account to enable him to get another ship and so help "a poor
fellow-not on the dole-in a state of starvation who walked from
Highbridge to Weston to see if I could give him a berth for him to
earn a crust of bread." This poor fellow was his half brother
Chapman who had been in the "XL" with him and with whom he had
sailed in other ships which had been lost from one cause or
another. There was further correspondence between Stokes and the
underwriters concerning the deviation of the vessel to Lamlash on
its journey to Kilkeel, as a deviation without good reason and not
reported to the underwriters is a matter which normally would make
a policy void. This was in September and although the underwriters
had been pressing Stokes to produce his receipts or their copies he
had failed to do so. On the 20th September, Stokes said, in his
letter of that date, to the underwriters: "I beg to say that I have
had an interview with the owners and they are quite willing to
accept the figure of the first insurance namely £400 in full
settlement of all claims ". This offer did not appeal to the
underwriters and on the 27th September, Messrs Coppack Bros, wrote
to Messrs Tyson Bros: "We have a reply from Capt Stokes-asking us
to get as much above £300 as possible in settlement." After
consideration the underwriters promised to pay £300 in full
settlement of all claims. After this promise was made the Board of
Trade requested that any payment should be withheld as the official
inquiries into the loss were incomplete, but the underwriters
having made a promise did in fact carry it out and paid Stokes the
sum of £300 in full settlement of all claims.
This sum was £100 less than the original valuation of £400,
£170-£200 less than the sum which Stokes said he had spent upon her
at Ramsey and £300 less than her insured value at the time of the
loss, and was accepted by him in full settlement. Stokes took no
further action to recover the remaining £300.
The Court finds that Stokes had in fact spent a sum not
exceeding £303 on the vessel and in that sum is included a sum of
£24 (part of a larger sum claimed by Stokes to have been so spent)
in respect of work done by the crew instead of by hired labour at
Ramsey. The ship was adequately insured on her first voyage and
there is no justification for the claim that £470-£500 was spent
upon her at Ramsey nor for the increase in the amount of the
insured value from £400 to £600. It is incomprehensible that had
Stokes had the receipts for the money, said to have been spent by
him, in the drawer in his cabin that he should have taken no steps
in the time at his disposal to have saved them, or that had such
receipts ever been in existence that he would not have been able to
obtain certified copies thereof.
The story of the loss of the vessel combined with the very
peculiar circumstances concerning the insurances effected upon her
is such that the Court has the gravest suspicion that the "XL" was
deliberately scuttled in an attempt to defraud the underwriters,
but the Court is unable on the evidence at its disposal to find
this as a fact, but the Court has no hesitation in saying that
there was no real desire shewn nor effort made by Stokes or Goff to
save this vessel when she was making water on the 4th and 5th July,
1930.
At the conclusion of the evidence Mr. G. St. C. Pilcher put a
series of questions to the Court. The questions and the answers
thereto given by the Court are shown below:-
1. When, from whom and for what sum of money was the motor
vessel "XL" acquired by Mrs. Edith Stokes?
Who acted as agent for Mrs. Stokes in the negotiations for the
purchase of the vessel?
The "XL" was acquired from Arthur Llewellyn Coffey on the 29th
April, 1930, for £130. William Bruford Stokes acted as agent for
his wife Edith Stokes.
2. What sum of money was spent by or on behalf of Mrs. Edith
Stokes upon repairs effected to and equipment of the vessel?
£172 2s. 9d., which figure includes the sum of £24, a proper
allowance for the work done by captain and crew.
3. Did Mrs. Edith Stokes manage the vessel herself or did she
depute the management of the vessel to some other and if so what
person?
No. The management of the vessel was deputed to William Bruford
Stokes.
4.-(a) What was the value of the vessel when she left
Ramsey?
(b) What insurances were effected upon or in connection
with the vessel when she last left (1) Ramsey, (2) Maryport, (3)
Drummore? By whom and in whose name were they effected?
(a) £292 2s. 9d.
(b1) £400.
(b2) £400.
(b3) £600.
All effected by William Bruford Stokes in his own name.
5. When did the vessel leave Ramsey, Isle of Man?
Had she been surveyed by a Board of Trade Surveyor?
If so, had all his requirements been complied with?
Was she then in good and seaworthy condition in hull and
machinery and equipment?
The vessel left Ramsey on the 4th of June, 1930, after having
been surveyed by a Board of Trade Surveyor, all of whose
requirements had been complied with. Hull and equipment were in
good and seaworthy condition but the auxiliary motor was
unreliable.
6. Who was in command of the vessel when she last left
Ramsey?
What was her port of destination?
Was any addition made to her crew after she left Ramsey?
If so what was the addition and why was it made?
William Bruford Stokes. Her port of destination was Maryport, at
which port J. R. B. Meek joined the vessel to augment the crew as
motorman and A.B.
7. When did the vessel arrive at Ayr?
Did she load any and if so what class and what amount of cargo
there? If so to whom and to what port was it consigned?
The vessel arrived at Ayr on the 22nd June, 1930, where she
loaded a cargo of 106 tons of coal consigned to William Annett, of
Kilkeel, Co. Down.
8. Was any and if so what change made in the command of the
vessel whilst she was at Ayr? If a change was made, what was the
reason for it?
Yes. William Bruford Stokes was discharged and re-engaged as
mate. John Borman Goff (mate) appointed master owing to the
indifferent health of W. B. Stokes.
9. Was the vessel in good and seaworthy condition as regards
hull, machinery and equipment when she left Ayr?
Had she a sufficient supply of lubricating oil for her
motor?
If the supply of lubricating oil was insufficient had this fact
been reported to the master or the mate by the motorman?
If so, were any, or any adequate, steps taken to replenish the
supply of lubricating oil?
Yes, with the exception that the motor was still unreliable. She
had a sufficient supply of lubricating oil.
10. When did the vessel leave Ayr? Did her motor function
efficiently when leaving the port?
She left Ayr on the 26th June, 1930.
No, her motor was still unreliable.
11. What was the intended destination of the vessel when she
left Ayr? Did she proceed to that destination or was she diverted
to Lamlash?
What was the reason for such alteration of her voyage, if it was
made? Was such alteration of voyage justified in the conditions
which prevailed ?
Her intended destination was Kilkeel but she did not proceed
there, being diverted en route to Lamlash. No
satisfactory reason was given for the alteration, which was not
justified in the conditions then prevailing.
12. Were any and if so what repairs effected to her hull and/or
machinery whilst she was at Lamlash? If any repairs were effected
by whom were they effected?
There were no repairs to her hull but there were small repairs
to her motor which were executed by Alexander Hamilton at a cost of
20s.
13. When did the vessel leave Lamlash? Was she then in good and
seaworthy condition as regards hull, machinery and equipment,
including life-saving apparatus and distress signals? Had she a
sufficient supply of motor lubricating oil for her intended voyage?
What was the draft of the vessel fore and aft on leaving
Lamlash?
The vessel left Lamlash on the 4th of July, 1930, at about 7
a.m. in a good and seaworthy condition with all the necessary
lifesaving apparatus and distress signals; her auxiliary motor was,
however, still unreliable and there was not a sufficient supply of
lubricating oil for the intended voyage. Her draft was 8ft. loins.
forward and 10ft. 2ins. aft.
14. What was her port of destination? Was it intended to call at
any and if so what port or ports on the voyage? If so, what was the
reason for calling at such port or ports?
Her port of destination was Kilkeel, Co. Down, and it was not
intended to call elsewhere.
15. What were the weather conditions when the vessel left
Lamlash?
(a) Direction and force of the wind?
(b) Visibility?
What was the state of the sea?
Weather was fine.
(a) Variable south to westerly winds varying from calm
to force 3.
(b) Good.
Sea was smooth.
16. When the vessel left Lamlash did she proceed under sail
and/or motor? What speed did she make and what was her course?
She left under sail and motor making 3 to 4 knots on a course
S.S.W. for Corsewell Point.
17. When the vessel left Lamlash was her small boat stowed on
board her or was it towing astern?
The boat was towing astern.
18. Was her motor stopped at any time after she left
Lamlash?
If so when and why was it stopped? Where was the vessel at this
time?
Was the motor ever re-started before she foundered and if so
when?
Yes, at about 1 p.m. on the 4th July, 1930, about 4 miles East
of Pladda through shortage of lubricating oil. The motor was
re-started by Meek after he found that the vessel was making
water.
19. Were there any and if so what material changes in-
(a) the weather conditions;
(b) the direction and force of the wind;
(c) the state of the sea
between the time when the vessel left Lamlash and the time when
she foundered?
(a) No material change except for slight patches of
fog.
(b) No change.
(c) No change.
20. During the course of the voyage did the vessel come into
contact with any floating or submerged object? If so what part of
the vessel was struck? Did she suffer damage from the contact and
if so what was the nature and extent of the damage? Did the damage,
if it occurred, permit water to enter the vessel in such quantity
as to cause the vessel to founder?
No. The Court is satisfied that the vessel did not come into
contact with any floating and/or submerged object.
21. Were there any, and if so how many sea connections in the
engine room through which water could enter or be admitted to the
vessel? What were the nature and dimensions of the sea
connections?
Yes, there were two ¾in. pipes fitted with lever cocks, one
fitted with rubber pipe connection to the engine, the other being
plugged above the cock.
22. How did the water enter the vessel? When and by whom was its
presence in the vessel first observed? Were prompt and proper
measures taken to close the aperture or apertures through which the
water was entering the vessel?
The water entered through some opening abaft the cargo hold. It
was first seen coming into the engine room by Charles Chapman,
A.B., during the afternoon of the 4th July, 1930. No proper steps
were taken to deal with this water.
23. How many pumps were there in the vessel? Where were they
situated? What type of pumps were they and what were their
respective dimensions? Were they in good condition and in efficient
working order?
There were two 5-inch deluge pumps in good and efficient
condition fitted at the after end of the cargo hold.
24. Were prompt and proper steps taken to expel the water from
the vessel? When did the pumping begin and when did it cease? Why
was the water not expelled from the vessel.
No. The Court is not satisfied that the pumps were ever
efficiently operated.
25. Were any distress signals exhibited by those on board the
vessel? If so what was their nature and when were they
exhibited?
If no distress signals were exhibited why were they not
exhibited?
It is possible that if flares had been shown they might not have
been seen and on the evidence the Court is unable to give a
definite answer.
26. Were all proper steps taken to save the vessel?
What steps were taken? Why were they not successful?
No proper steps were taken to save the vessel.
27. At what time was the vessel's small boat launched?
When did the crew embark in the small boat?
The boat had been in tow since the "XL" had sailed from Lamlash
and the crew embarked therein on the 5th July, 1930, about 4.15
a.m.
28. At what time and where did the motor vessel "XL"
founder?
About 4.45 a.m. on the 5th July, 1930, in 55° 7' 12" N. Lat. 5°
1' 48" W. Long.
29. What was the cause of the foundering of the motor vessel
"XL" ?
The flooding of the vessel with sea water.
30. Was the loss of the motor vessel "XL" caused or contributed
to by the wrongful act or default of John Borman Goff, master,
William Bruford Stokes, mate, Charles Chapman, A.B., John Robert
Buller Meek, A.B. and motorman, or any and if so which of them?
The loss of the "XL" was caused by the grave default of John
Borman Goff, master, and William Bruford Stokes, mate and part
owner, by their failure to take the necessary steps to save the
vessel when she was making water on the 4th and 5th July, 1930.
Dated 29th day of May, 1931.
HERBERT METCALFE, Judge.
We concur,
| | JOHN ELMES,
W. A. SPLATT,
T. H. BLAKER,
| Assessors. |
(Issues by the Board of Trade in London
on Thursday, the 6th day of August, 1931.)
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